3120 Gone BAD

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Disclaimer: I did not do the port work on this saw!!!

A quick history here. This 3120 was bought brand new back in '04 by another forum member. It was ported, muffler modded, and the timing advanced. Shortly there after the offset keyway sheared. It hasn't run right since that time and has just sat all these years. I have it to sort it out and get it running good. I pulled a compression check and only got 110-115 PSI. However, the rings still look like brand new, with the little machine lines still in them. This saw never even got broken in.

None of the ports were widened. However, the exhaust was raised A LOT. The transfers were also raised considerably, and the intake lowered. I will be putting a degree wheel on it to see where it sets.

What happened to this saw? Notice all the odd markings in the cylinder and piston. Did this saw get real hot at one time, but not enough to seize? You can see the shape of the exhaust port roof on the piston skirt where the piston is at TDC. Was the port not deburred and beveled after porting, and marked the piston? There's one line to the right of the exhaust port on the cylinder wall that I can feel. Why is the compression so low? Exhaust too high?


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It was only raised at the cylinder wall, and not tapered out to the flange.
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Not widened at the cylinder wall at all. You see some finish sanding marks towards the flange. It was not widened.
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Markings above the intake.
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Better check the timing and jetting for the new piston and cylinder.
 
uuuhhhhh...first of all, everything is left pretty rough, and by the looks of it they didn't realy even do the numbers it sounds like....i'd say turn it into a cup holder and buy a new jug.
 
uuuhhhhh...first of all, everything is left pretty rough, and by the looks of it they didn't realy even do the numbers it sounds like....i'd say turn it into a cup holder and buy a new jug.

A degree wheel will answer that. The roughness can be cleaned up. BTW, the muffler and exhaust gasket weren't even port matched.
 
The numbers aren't near as bad as I feared. The transfers are higher than I'd like but I think it should be able to be made to run well.

Exhaust 96° - 168° Duration
Transfers 117° - 126° Duration
Intake 81° - 162° Duration
Blowdown - 21°

I'm still really curious about all the strange markings on the P&C. I'm suspicious that the ports were not deburred and beveled after porting, and consequently scrathed the piston. I see no bevel on the ports at all. The piston is not really hurt though. Pictures make things look worse than they are.

I think the markings in the cylinder are due to extreme heat. I suspect a good oil was being used and prevented seizure. Or, it was just shy of melting temps.

I'm stumped on why the compression is so low. The oil on the piston was really gooey and sticky. It may have been years since it ran. I'm thinking I'll clean things up, hone the cylinder, and put it back together and see what happens.
 
I wondering if by raising the exhaust port, the saw no longer had sufficient torque. Then the operator lugged it to it's death.
 
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