Hello All,
I spent yesterday re-thinking our wintertime ventilation situation. After much research and amazement at the cost of things, I found a new fan at WalMart for $12. It is a high velocity (high speed), 9-inch fan with aluminum blades. I took it apart and made a shroud for it. It will mount on the ceiling with only the back grate sticking out. It will replace out the two computer fans that I now have powering air through 8" flexible ducting to the upstairs. The computer fans have been very reliable (rated at 5000hrs) and have ran for three winters full-time from cold-snap to spring-frost. I'm guessing they have run for 12,000 hrs or better without a single squeak. I'm hoping that this new fan will last just as well if I keep it oiled.
I was hoping to be able to balance the fan by putting bits of solder on it, but it's proven a difficult task because the center of gravity if in front of the axle. I cannot find a way to string it up. I did readjust the pitch of the blades and got them all into line with each other. There is still some vibration present at super-high speed.
Last night I thought. The fan is mounted on a 12" by 12" frame. I will place this frame inside a 13" or 14" frame that is mounted on the ceiling. I will attach the fan frame to the mounting frame with strips of fiber reinforced rubber strips (army surplus). I thought I if I used rubber all the way around, it would transmit too many vibrations, so I think I'm going to use old bed-sheet strips to fill in the gap and paint the strips with latex to seal in the air.
I'm also going to rework the ducting for smoother flow. I'm hoping to get 200cfm with 70 watts instead of the current 80cfm with 44 watts. The overall objective is to keep the downstairs cooler while burning a greater percentage of firewood to pellets.We'll see.
EDIT -- I finished the duct fan. It came out really nice. No vibration transferred to the house at all. It will look better once I trim the fabric and paint it white (including the grille). The fiber reinforced rubber was too sturdy (military surplus, huh.)! I had to cut strips, then cut a "Z" in them to get enough flexibility. I also reworked the distribution box in the upstairs closet. I used cardboard and duct tape to coerce the air towards the grille. I also bent the fins on the grille to keep the air traveling down the hallway better. WHAT A DIFFERENCE!! Before, I could barely feel the air moving. Now, It feels like you are sitting in front of a fan, go figure. I estimate at least triple the flow and only twice the wattage. I am going to buy a spare fan tonight; $12 is cheap insurance.
I spent yesterday re-thinking our wintertime ventilation situation. After much research and amazement at the cost of things, I found a new fan at WalMart for $12. It is a high velocity (high speed), 9-inch fan with aluminum blades. I took it apart and made a shroud for it. It will mount on the ceiling with only the back grate sticking out. It will replace out the two computer fans that I now have powering air through 8" flexible ducting to the upstairs. The computer fans have been very reliable (rated at 5000hrs) and have ran for three winters full-time from cold-snap to spring-frost. I'm guessing they have run for 12,000 hrs or better without a single squeak. I'm hoping that this new fan will last just as well if I keep it oiled.
I was hoping to be able to balance the fan by putting bits of solder on it, but it's proven a difficult task because the center of gravity if in front of the axle. I cannot find a way to string it up. I did readjust the pitch of the blades and got them all into line with each other. There is still some vibration present at super-high speed.
Last night I thought. The fan is mounted on a 12" by 12" frame. I will place this frame inside a 13" or 14" frame that is mounted on the ceiling. I will attach the fan frame to the mounting frame with strips of fiber reinforced rubber strips (army surplus). I thought I if I used rubber all the way around, it would transmit too many vibrations, so I think I'm going to use old bed-sheet strips to fill in the gap and paint the strips with latex to seal in the air.
I'm also going to rework the ducting for smoother flow. I'm hoping to get 200cfm with 70 watts instead of the current 80cfm with 44 watts. The overall objective is to keep the downstairs cooler while burning a greater percentage of firewood to pellets.We'll see.
EDIT -- I finished the duct fan. It came out really nice. No vibration transferred to the house at all. It will look better once I trim the fabric and paint it white (including the grille). The fiber reinforced rubber was too sturdy (military surplus, huh.)! I had to cut strips, then cut a "Z" in them to get enough flexibility. I also reworked the distribution box in the upstairs closet. I used cardboard and duct tape to coerce the air towards the grille. I also bent the fins on the grille to keep the air traveling down the hallway better. WHAT A DIFFERENCE!! Before, I could barely feel the air moving. Now, It feels like you are sitting in front of a fan, go figure. I estimate at least triple the flow and only twice the wattage. I am going to buy a spare fan tonight; $12 is cheap insurance.
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